T.Roller
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The pics I posted of the 026 muffler were on a stock saw. It responded very well.
In the past, I have seen too much muff opening make it difficult to set idle + / or diminish throttle response. And, sometimes, not increase performance.
Please keep in mind, these are not ported saws, they are stock saws, just looking for a little bump in performance at a low cost.
Only time I've seen idling issues is with very large front exit holes.
I did a large front exit on my 395 just to play around with. I had to turn the low side out 3 turns but it would idle all day long. It's ported thoView attachment 133269 View attachment 133270 View attachment 133271 View attachment 133272
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Only a muffler mod on a pure bone stock, brand new saw
No idling or tuning issues and a bunch of people at the Ct gtg thought it was ported because it made such an improvement over a saw with a stock muffler
I’ve done a bunch of them, ported, stock, it doesn’t matter, letting them breathe makes them run betterer
Is the gage good? That seems low, hope it works out! Have had a few gages that went badMaking more progress on the 064. I checked the compression for the heck of it and it’s only 110 psi. I hope it is because it’s not broken in yet.![]()
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Have you ran it with just one of those ports? One of those holes is the same size a my 250r with a 350 kit exhaust!View attachment 133269 View attachment 133270 View attachment 133271 View attachment 133272
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Only a muffler mod on a pure bone stock, brand new saw
No idling or tuning issues and a bunch of people at the Ct gtg thought it was ported because it made such an improvement over a saw with a stock muffler
I’ve done a bunch of them, ported, stock, it doesn’t matter, letting them breathe makes them run betterer
That's way low, I'd check it with another gauge to make sure yours is right. If it is than you'lL need to tear it down.Making more progress on the 064. I checked the compression for the heck of it and it’s only 110 psi. I hope it is because it’s not broken in yet.![]()
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Sent from my iPhone using Tapatalk
Is the gage good? That seems low, hope it works out! Have had a few gages that went bad
Good way to bend or break a crank, ask how i knowStart it up.....give it a little rev and trip the break. Once or twice and it's not coming off.
NO Locktite.
That's way low, I'd check it with another gauge to make sure yours is right. If it is than you'lL need to tear it down.
I think the gauge is good, I checked the compression on a 032 and it read 140 psi.
The cylinder on the 064 had aluminum transfer on it and i cleaned it up.
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I ran my clone 372 yesterday after doing some port work, it gained but wasn’t quite what
I was looking for, so today after work I did some more porting 100/120/75 going to see how it runs after that! If I am not happy going to machine .020-.030 out of the band, to gain some compression, lifting the exhaust to 100 from 107 it lost 10 psi, still had 165 psi, I didn’t want to lower the intake, in case I machine .030, that would probably be ideal, but trying to learn