Well last night i put an air test on it before bed, it held positive and negative. Today after dinner i filled it up and pulled the crap out of it.
nothin...
Nice managed to switch fuel and impulse around... switched that back right quick
I set the carb to factory 1 turn on L and 1.25 on high. Left the idle alone cause i dont know what the factory is on that.
try again and she fired right up, high idle off and shes idling at like 3800 from my previous idle screw setting.
Turned idle down to 2700 or so, just felt a little lean on the L so gave that 1/4 turn out.
Nice steady idle, didnt smoke after letting it idle and then blipping the throttle anymore. Also it sounded like it was firing more, kinda like when you hear a truck/car engine missing, that same kind of lack of noise was gone now.
throttle response was great, took it to the wood pile and layed into it. Was 4 stroking on and off in the cut, just perfect, didnt even have to touch the H screw, at least for now.
so far she seems fixed.
couple things i want to get before i bring it out in the bush
New tank vent insert, gut it and put a stihl/echo vent in the airbox
mine is cracked from pulling on it. I didnt trust the husky vent cause it was incredibly hard to pass air through it so i removed the check and kept one puck which felt much better. It will leak for now but slow.
new fuel line
Im using the yellow line that is slightly smaller, i managed to put some shrink wrap on it to make a tight fit on the tank and it holds gas back. However the bent is a little aggressive and the line kinks easily, i dont want to lean out in the bush so id rather get a new line and have the factory bends that prevent kinking.
Thats it, after that its a full out test. What do you guys think?