View attachment 351577 View attachment 351578 View attachment 351579 View attachment 351580 View attachment 351581 Well I cleaned up the seal seat. Put a seal in and it didn’t heave at all. Looks pretty good actually. I was very meticulous when it came to cleaning the seat and chamfering the entrance. Idk. I think it should be tested for testing purposes.
View attachment 351577 View attachment 351578 View attachment 351579 View attachment 351580 View attachment 351581 Well I cleaned up the seal seat. Put a seal in and it didn’t heave at all. Looks pretty good actually. I was very meticulous when it came to cleaning the seat and chamfering the entrance. Idk. I think it should be tested for testing purposes.
Update. I ran 7-8 tanks through the saw and all was well. Until it suddenly went way lean. Figured my seal fix went kaput. Today I finally got around to pressure testing it.
Here’s the video.
Leaking the opposite side of the fix.
But what’s funny is it’s the opposite side as the epoxy. The side with the repair isn’t leaking at all. Is it a bad seal? Is it ever so slightly out of round that it pancaked the top side. Is the seal pinched funny when pressing in?Using epoxy to prevent an air leak is never a good idea.
If I can see the needle move looking at it for 5 seconds, I try and fix it. In my experience, leaks that cause running issues are noticeable on the needle. They usually only pump up to less than 5 psi and will fall off quickly to under 2 psi within a few seconds.But what’s funny is it’s the opposite side as the epoxy. The side with the repair isn’t leaking at all. Is it a bad seal? Is it ever so slightly out of round that it pancaked the top side. Is the seal pinched funny when pressing in?
I feel like further investigation is required and hoped for some ideas.
Also the leak is slow. Barely nicking a psi every few seconds. Can anyone elaborate how much of a leak is needed to obviously know a running saw is leaning out. I saw this because I’m thinking there’s something else going on here.
I fixed an 066 for @jacob j. like that. I don’t see any reason it won’t lastSo I added some motoseal to the opposite side of the jb epoxy fix. Pulled vacuum for 5 minutes or so then just pumped it every 5 minutes or so. After an hour I can back and checked it and it was holding vacuum.
Tomorrow I’ll clean up the excess motoseal and throw some pressure at it and see how she holds.
I fixed an 066 for @jacob j. like that. I don’t see any reason it won’t last