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- Dec 31, 2015
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Still runs too lolMeh, ive done worse. Lol.
Took it apart to change carbs and it had cracked again. Was still barely holding on, certainly leaking air the last time i ran it. I used more JB this timeStill runs too lol
Took it apart to change carbs and it had cracked again. Was still barely holding on, certainly leaking air the last time i ran it. I used more JB this time![]()
Thanks Matt
@Dookie...rrr @Duke Thieroff
You know, I was only joking that time when I said you could use a chunk of JB Weld as a carburetor...
Honestly, you gotta give the guy credit. Rather ingenious and a solid attempt for someone that may not have had the understanding of the 395 swap.I think that's pretty awesome, actually. The sheer amount of planning and effort that went into such a crappy repair is quite impressive in my book.
Don't give me any ideas....If Dookie wouldn't have run out of JB Weld he could have put a reed box on there. Lol
Never vac tested.....the loose wobble of the block against the intake clued me inSo it doesn’t seal? Are the other ports hacked?
There it is...didn't look like there's a husky part number for it, just a pieced together kit....Thanks Matt
@Dookie...rrr @Duke Thieroff
Haha yep.
View attachment 320384
Meh, ive done worse. Lol.
I think Chris had a good 394 jug, so no conversion kit needed. the jug that was ..uh...modded....appears to be an AM 395 jug.
not sure I would have put a good 394 jug on that saw lol... them things are getting more rare
Don't give me any ideas....
There it is...didn't look like there's a husky part number for it, just a pieced together kit....