Intake boot was seated properly pulled the jug and checked it again today put a new one on it for the heck of it and resealed cylinder again. Going to try it again tomorrow
I did it a couple times before and it held pressure and vacuum but it kept developing a leak before because the bearing pocket was worn on the PTO side. Now with a new case it was holding fine when I first put it together haven't checked since but been doing this the entire time. No erratic...
Can someone please try to help me out here and see what the heck could be causing this weird running issue with this conversion. I have changed and swapped a lot of pieces trying to figure it out I was just curious if someone else had any input on what could be wrong. It runs good for 1-2 short...
Hybrid made 3 cuts then clutch and oil pump went boom. Stinks it was a brand new clutch too I forgot to put the washer behind the clutch. That one stings
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